FIR 1 - INSPECTION REPORT

Permit Holder: Merit Energy Company, LLC Well Name/No: Jenkins Permit: 9343
Lease Name: Jenkins 2 Sec: 21 Twp: 10N Range 27W
GPS Well Location: Latitude: 35.51747 Longitude: -93.87315 Field: WHITE OAK  
Lease/Tank Battery: Latitude: 35.51751 Longitude: 93.87319 County: FRANKLIN  
Entrance from nearest 911 address, public street or highway Lone Oak Road
Status:
Well equipment operational: Equipment plumbed properly: Excess equipment on lease:
Signs: At lease entrance:
At tank battery:
At well:
Signage compliance:

NoTypeConstructionSizeLeaksRemarks
1Fluids TankFiberglassOther Size 10' round x 10' h = 140 bbls
2SeparatorSteel Welded   

Tank Containment:
Dimensions: Length: 0 Width: 0 Diameter: 16 Height: 6 Capacity (bbls): 215
Capacity compliance: Breaches/Erosion: Excessive vegetation present: Compliance agreement:
Containment Conditions: Fluids Present:
Well Site Compressor:
Is it in compliance?
Trash/Debris:
Use as storage area:
Unusual equipment:
Excessive erosion:
If yes to any, explain:
Entry Gate Present:
  Gate locked on arrival:
Gate locked on departure:
Is spill or discharge of drilling, completion or produced fluids present:
 
If yes, did spill or discharge of drilling, completion or produced fluids occur or travel off the well pad:
(If yes, complete FIR 5)
Compliance Summary Remarks:
Producing, large drain pipe for produced water tank is broken off, produced fluids are draining directly into containment. Large area around containment was wet, from fluids being drained onto ground, just prior to this inspection. Operator contacted. No enforcement at this time.MP

Inspected by: DAYMON BLOUNT   Date:  9/9/2020 10:56:00 AM
Review for NNC or NOV:
If yes, check one
Ref #: Date: 9/17/2020
ADEQ referral:
Date of referral:  __________