FIR 1 - INSPECTION REPORT

Permit Holder: Oxley Energy, LLC Well Name/No: Brashears Permit: 35917
Lease Name: Brashears 5-33 Sec: 33 Twp: 9N Range 26W
GPS Well Location: Latitude: 35.40232 Longitude: -93.76892 Field: AETNA  
Lease/Tank Battery: Latitude: 0 Longitude: 0 County: FRANKLIN  
Entrance from nearest 911 address, public street or highway Mallard Lane
Status:
Well equipment operational: Equipment plumbed properly: Excess equipment on lease:
Signs: At lease entrance:
At tank battery:
At well:
Signage compliance:

NoTypeConstructionSizeLeaksRemarks
1Fluids TankFiberglass100 12' x 5'
2SeparatorSteel Welded   
3SeparatorSteel Welded   

Tank Containment:
Dimensions: Length: 0 Width: 0 Diameter: 24 Height: 2 Capacity (bbls): 161
Capacity compliance: Breaches/Erosion: Excessive vegetation present: Compliance agreement:
Containment Conditions: Fluids Present:
Well Site Compressor:
Is it in compliance?
Trash/Debris:
Use as storage area:
Unusual equipment:
Excessive erosion:
If yes to any, explain:
Entry Gate Present:
  Gate locked on arrival:
Gate locked on departure:
Is spill or discharge of drilling, completion or produced fluids present:
 
If yes, did spill or discharge of drilling, completion or produced fluids occur or travel off the well pad:
(If yes, complete FIR 5)
Compliance Summary Remarks:
TA. Fluid test. Tubing Fluid level was 4535 with 468 PSI. On the casing we shot it 5 different times on both sides and could not get an accurate reading. Its showing 28.6 PSI with a fluid depth of 51 feet. Every time he shot the casing you could hear it hit right there. Fluid level should not be that high on casing. Seems to have some type of restriction going on like something has moved. I put on FIR that it failed test. Other remarks are that location and lease road have vegetation. H.S

Inspected by: HAYDEN SLAYTON   Date:  7/27/2023 3:09:00 PM
Review for NNC or NOV:
If yes, check one
Ref #: Date: __________
ADEQ referral:
Date of referral:  __________