FIR 1 - INSPECTION REPORT

Permit Holder: Merit Energy Company, LLC Well Name/No: Holden Permit: 37355
Lease Name: Holden 3-23 Sec: 23 Twp: 9N Range 29W
GPS Well Location: Latitude: 35.45202 Longitude: -94.04413 Field: CECIL  
Lease/Tank Battery: Latitude: 35.45215 Longitude: 94.04393 County: FRANKLIN  
Entrance from nearest 911 address, public street or highway Hwy 96
Status:
Well equipment operational: Equipment plumbed properly: Excess equipment on lease:
Signs: At lease entrance:
At tank battery:
At well:
Signage compliance:

NoTypeConstructionSizeLeaksRemarks
1Fluids TankFiberglassOther Size 7' round x 7' h = 48 bbls
2SeparatorSteel Welded   
3SeparatorSteel Welded   
4SeparatorSteel Welded   

Tank Containment:
Dimensions: Length: 0 Width: 0 Diameter: 10 Height: 4.5 Capacity (bbls): 63
Capacity compliance: Breaches/Erosion: Excessive vegetation present: Compliance agreement:
Containment Conditions: Fluids Present:
Well Site Compressor:
Is it in compliance?
Trash/Debris:
Use as storage area:
Unusual equipment:
Excessive erosion:
If yes to any, explain:
Entry Gate Present:
  Gate locked on arrival:
Gate locked on departure:
Is spill or discharge of drilling, completion or produced fluids present:
 
If yes, did spill or discharge of drilling, completion or produced fluids occur or travel off the well pad:
(If yes, complete FIR 5)
Compliance Summary Remarks:
FIR is for a spill reported by XTO. Heavy floods had location completely under water, tank and containment were overturned, plumbing at meter run was damaged. Tank and containment have been repaired, damaged plumbing has been repaired, clean location is back to producing.

Inspected by: DAYMON BLOUNT   Date:  7/2/2019 9:10:00 AM
Review for NNC or NOV:
If yes, check one
Ref #: Date: __________
ADEQ referral:
Date of referral:  __________