FIR 1 - INSPECTION REPORT

Permit Holder: Oxley Energy, LLC Well Name/No: Carter Permit: 25874
Lease Name: Carter 1-4 Sec: 4 Twp: 8N Range 26W
GPS Well Location: Latitude: 35.38921 Longitude: -93.76703 Field: AETNA  
Lease/Tank Battery: Latitude: 0 Longitude: 0 County: FRANKLIN  
Entrance from nearest 911 address, public street or highway Kirk Road
Status:
Well equipment operational: Equipment plumbed properly: Excess equipment on lease:
Signs: At lease entrance:
At tank battery:
At well:
Signage compliance:

NoTypeConstructionSizeLeaksRemarks
1Fluids TankFiberglass  16' round x 5' h = 179 bbls
2Fluids TankOther Types  15 bbl used oil tank inside containment
3SeparatorSteel Welded   
4SeparatorSteel Welded   
5SeparatorSteel Welded   

Tank Containment:
Dimensions: Length: 0 Width: 0 Diameter: 30 Height: 2.25 Capacity (bbls): 283
Capacity compliance: Breaches/Erosion: Excessive vegetation present: Compliance agreement:
Containment Conditions: Fluids Present:
Well Site Compressor:
Is it in compliance?
Trash/Debris:
Use as storage area:
Unusual equipment:
Excessive erosion:
If yes to any, explain: Old ajax compressor does not appear to be operational, plumbing is rotted and broken, plumbing to used oil tank is leaking a small amount of oil onto ground.
Entry Gate Present:
  Gate locked on arrival:
Gate locked on departure:
Is spill or discharge of drilling, completion or produced fluids present:
 
If yes, did spill or discharge of drilling, completion or produced fluids occur or travel off the well pad:
(If yes, complete FIR 5)
Compliance Summary Remarks:
Fluid level test conducted on 07/12 - 3740' @ 121 PSI, pump jack at wellhead, containment ring does not have a liner, moderate oil on ground around wellhead, excessive vegetation (small trees) growing around wellhead.

Inspected by: DAYMON BLOUNT   Date:  7/12/2018 10:12:00 AM
Review for NNC or NOV:
If yes, check one
Ref #: Date: __________
ADEQ referral:
Date of referral:  __________