FIR 1 - INSPECTION REPORT
Permit Holder:
Standard Oil Co of LA
Well Name/No:
Umsted, Sid
Permit:
4365
Lease Name:
Umsted, Sid 23
Sec:
32
Twp:
15S
Range
15W
GPS Well Location:
Latitude:
33.37624
Longitude:
-92.67426
Field:
WILDCAT
Lease/Tank Battery:
Latitude:
0
Longitude:
0
County:
OUACHITA
Entrance from nearest 911 address, public street or highway
Status:
Completing
New not producing
Operating
Old not producing
Not found
Single well pad
Mutiple well pad
NA
Well equipment operational:
Equipment plumbed properly:
Excess equipment on lease:
Yes
No
NA
Yes
No
NA
Yes
No
Signs:
At lease entrance:
Yes
No
At tank battery:
Yes
No
NA
At well:
Yes
No
NA
Signage compliance:
Yes
No
No
Type
Construction
Size
Leaks
Remarks
No Vessels Found For This Inspection
Tank Containment:
Earthen
Metal ring
Tank in tank
No Tanks
Other
Dimensions:
Length:
0
Width:
0
Diameter:
0
Height:
0
Capacity (bbls):
0
Capacity compliance:
Breaches/Erosion:
Excessive vegetation present:
Compliance agreement:
Yes
No
NA
Yes
No
NA
Yes
No
NA
Yes
No
NA
Containment Conditions:
Fluids Present:
Yes
No
Produced fluids
Storm water
Waste oil
NA
Other
Well Site Compressor:
Yes
No
Is it in compliance?
Yes
No
NA
Trash/Debris:
Yes
No
Use as storage area:
Yes
No
Unusual equipment:
Yes
No
Excessive erosion:
Yes
No
If yes to any, explain:
Entry Gate Present:
Yes
No
Gate locked on arrival:
Yes
No
Gate locked on departure:
Yes
No
Is spill or discharge of drilling, completion or produced fluids present:
Yes
No
If yes, did spill or discharge of drilling, completion or produced fluids occur or travel off the well pad:
Yes
No
NA
(If yes, complete FIR 5)
Compliance Summary Remarks:
Checked pressure on well bore this morning and it was 5psig. Had to call a mechanic in to work on the oil rig to get it started. Got it started at 0955hrs. Started in the well bore and tagged bottom at 2415ft(77joints) around 1045hrs. Started circulating at 1100hrs. Got back just a small amount of wood and rubber on the return screen. Stopped circulating at 1210hrs. Starting in with the cement for the first plug at 1220hrs. Plug set at 1230hrs. Put in 15 sacks which made up 100ft. 2415ft to 2315ft. Pulled out 10 joints of tubing and started the reverse flow to make sure cement was out of the tubing. Lost a little fluid during this time. The back flow from the well has stopped. Pulled out another 27 joints. Left 40 joints in the well bore. We are at 1252ft now. Filled tubing back up and checked after 30 minutes. Lost around 2bbls of fluid during this time.
Inspected by:
GLEN OWENS
Date:
6/8/2022 3:53:00 PM
Review for NNC or NOV:
Yes
No
If yes, check one
NNC
NOV
DNI
NA
Ref #:
Date:
__________
ADEQ referral:
Yes
No
Date of referral:
__________
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