FIR 1 - INSPECTION REPORT
Permit Holder:
Standard Oil Co of LA
Well Name/No:
Umsted, Sid
Permit:
4365
Lease Name:
Umsted, Sid 23
Sec:
32
Twp:
15S
Range
15W
GPS Well Location:
Latitude:
33.37624
Longitude:
-92.67426
Field:
WILDCAT
Lease/Tank Battery:
Latitude:
0
Longitude:
0
County:
OUACHITA
Entrance from nearest 911 address, public street or highway
Status:
Completing
New not producing
Operating
Old not producing
Not found
Single well pad
Mutiple well pad
NA
Well equipment operational:
Equipment plumbed properly:
Excess equipment on lease:
Yes
No
NA
Yes
No
NA
Yes
No
Signs:
At lease entrance:
Yes
No
At tank battery:
Yes
No
NA
At well:
Yes
No
NA
Signage compliance:
Yes
No
No
Type
Construction
Size
Leaks
Remarks
No Vessels Found For This Inspection
Tank Containment:
Earthen
Metal ring
Tank in tank
No Tanks
Other
Dimensions:
Length:
0
Width:
0
Diameter:
0
Height:
0
Capacity (bbls):
0
Capacity compliance:
Breaches/Erosion:
Excessive vegetation present:
Compliance agreement:
Yes
No
NA
Yes
No
NA
Yes
No
NA
Yes
No
NA
Containment Conditions:
Fluids Present:
Yes
No
Produced fluids
Storm water
Waste oil
NA
Other
Well Site Compressor:
Yes
No
Is it in compliance?
Yes
No
NA
Trash/Debris:
Yes
No
Use as storage area:
Yes
No
Unusual equipment:
Yes
No
Excessive erosion:
Yes
No
If yes to any, explain:
Entry Gate Present:
Yes
No
Gate locked on arrival:
Yes
No
Gate locked on departure:
Yes
No
Is spill or discharge of drilling, completion or produced fluids present:
Yes
No
If yes, did spill or discharge of drilling, completion or produced fluids occur or travel off the well pad:
Yes
No
NA
(If yes, complete FIR 5)
Compliance Summary Remarks:
Checked well flow back pressure and it was 50psig. Started in the hole and tagged something around 703ft at 0820hrs. Installed power swivel and went down a couple joints and then removed the power swivel. Went back down and tagged again around 805ft and installed power swivel again. Went down a couple joints and removed power swivel again. Did not get anything back out of the well onto the screen. Started back down and the joints fell in smoothly and got down to 2403ft before tagging up on bottom. Total of 72 joints. Circulated for about an hour. Pulled tubing and collars out and removed the collars and installed 3 3/4" drill bit on the tubing and went back down the well bore. At around 24 joints in the oil rig shut down. Fuel filters seemed to have clogged around 1730hrs.
Inspected by:
GLEN OWENS
Date:
6/7/2022 8:56:00 AM
Review for NNC or NOV:
Yes
No
If yes, check one
NNC
NOV
DNI
NA
Ref #:
Date:
__________
ADEQ referral:
Yes
No
Date of referral:
__________
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