FIR 1 - INSPECTION REPORT
Permit Holder:
Standard Oil Co of LA
Well Name/No:
Umsted, Sid
Permit:
4365
Lease Name:
Umsted, Sid 23
Sec:
32
Twp:
15S
Range
15W
GPS Well Location:
Latitude:
33.37624
Longitude:
-92.67426
Field:
WILDCAT
Lease/Tank Battery:
Latitude:
0
Longitude:
0
County:
OUACHITA
Entrance from nearest 911 address, public street or highway
Status:
Completing
New not producing
Operating
Old not producing
Not found
Single well pad
Mutiple well pad
NA
Well equipment operational:
Equipment plumbed properly:
Excess equipment on lease:
Yes
No
NA
Yes
No
NA
Yes
No
Signs:
At lease entrance:
Yes
No
At tank battery:
Yes
No
NA
At well:
Yes
No
NA
Signage compliance:
Yes
No
No
Type
Construction
Size
Leaks
Remarks
No Vessels Found For This Inspection
Tank Containment:
Earthen
Metal ring
Tank in tank
No Tanks
Other
Dimensions:
Length:
0
Width:
0
Diameter:
0
Height:
0
Capacity (bbls):
0
Capacity compliance:
Breaches/Erosion:
Excessive vegetation present:
Compliance agreement:
Yes
No
NA
Yes
No
NA
Yes
No
NA
Yes
No
NA
Containment Conditions:
Fluids Present:
Yes
No
Produced fluids
Storm water
Waste oil
NA
Other
Well Site Compressor:
Yes
No
Is it in compliance?
Yes
No
NA
Trash/Debris:
Yes
No
Use as storage area:
Yes
No
Unusual equipment:
Yes
No
Excessive erosion:
Yes
No
If yes to any, explain:
Entry Gate Present:
Yes
No
Gate locked on arrival:
Yes
No
Gate locked on departure:
Yes
No
Is spill or discharge of drilling, completion or produced fluids present:
Yes
No
If yes, did spill or discharge of drilling, completion or produced fluids occur or travel off the well pad:
Yes
No
NA
(If yes, complete FIR 5)
Compliance Summary Remarks:
Upon arrival there was backflow out of the 7" of around 20psig. Installed the 4th collar and started drilling at 0840hrs. Started at 162ft and ended at 1081ft at 1600hrs. It was 30 joints total. Took the power swivel off 1510hrs at around 663ft. The joint were falling right in at this point. Got a little rubber wood and burlap out up to 663ft and then did not get anything out the rest of the day. Circulated the hole until it cleaned up then pulled out tubing except for 4 drill collars and half a joint which left 145ft in the hole for the weekend. Closed the BOP and the valve that was installed on top of the tubing.
Inspected by:
GLEN OWENS
Date:
6/3/2022 2:02:00 PM
Review for NNC or NOV:
Yes
No
If yes, check one
NNC
NOV
DNI
NA
Ref #:
Date:
__________
ADEQ referral:
Yes
No
Date of referral:
__________
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