FIR 1 - INSPECTION REPORT

Permit Holder: Merit Energy Company, LLC Well Name/No: Wharton Permit: 36555
Lease Name: Wharton 3-35 Sec: 35 Twp: 9N Range 22W
GPS Well Location: Latitude: 35.3872 Longitude: -93.31156 Field: KNOXVILLE  
Lease/Tank Battery: Latitude: 0 Longitude: 0 County: JOHNSON  
Entrance from nearest 911 address, public street or highway
Status:
Well equipment operational: Equipment plumbed properly: Excess equipment on lease:
Signs: At lease entrance:
At tank battery:
At well:
Signage compliance:

NoTypeConstructionSizeLeaksRemarks
1Fluids TankFiberglass150 12' x 7'
2Separator    
3Other TanksFiberglassOther Size 5' x 4' compressor blow down tank.

Tank Containment:
Dimensions: Length: 0 Width: 0 Diameter: 24 Height: 3 Capacity (bbls): 242
Capacity compliance: Breaches/Erosion: Excessive vegetation present: Compliance agreement:
Containment Conditions: Fluids Present:
Well Site Compressor:
Is it in compliance?
Trash/Debris:
Use as storage area:
Unusual equipment:
Excessive erosion:
If yes to any, explain:
Entry Gate Present:
  Gate locked on arrival:
Gate locked on departure:
Is spill or discharge of drilling, completion or produced fluids present:
 
If yes, did spill or discharge of drilling, completion or produced fluids occur or travel off the well pad:
(If yes, complete FIR 5)
Compliance Summary Remarks:
Compressor tank hose popped off and leaked oil into containment. Oil has seeped outside of containment ring through gravel. Tank valve was shut before time of inspection stopping leak.

Inspected by: DEREK GOODMAN   Date:  4/11/2022 3:02:00 PM
Review for NNC or NOV:
If yes, check one
Ref #: Date: __________
ADEQ referral:
Date of referral:  __________