FIR 1 - INSPECTION REPORT

Permit Holder: Merit Energy Company, LLC Well Name/No: Barton, Paul Permit: 37248
Lease Name: Barton, Paul 4-21 Sec: 21 Twp: 9N Range 28W
GPS Well Location: Latitude: 35.44279 Longitude: -93.9688 Field: CECIL  
Lease/Tank Battery: Latitude: 35.44296 Longitude: 93.96865 County: FRANKLIN  
Entrance from nearest 911 address, public street or highway Hwy 96
Status:
Well equipment operational: Equipment plumbed properly: Excess equipment on lease:
Signs: At lease entrance:
At tank battery:
At well:
Signage compliance:

NoTypeConstructionSizeLeaksRemarks
1Fluids TankFiberglass210 10' round x 15' h = 210 bbls
2Fluids TankFiberglassOther Size 15 bbl used oil tank with containment
3Fluids TankOther TypesOther Size 200 gal plastic used oil tank
4SeparatorSteel Welded   
5SeparatorSteel Welded   
6SeparatorSteel Welded   

Tank Containment:
Dimensions: Length: 0 Width: 0 Diameter: 28 Height: 3.5 Capacity (bbls): 384
Capacity compliance: Breaches/Erosion: Excessive vegetation present: Compliance agreement:
Containment Conditions: Fluids Present:
Well Site Compressor:
Is it in compliance?
Trash/Debris:
Use as storage area:
Unusual equipment:
Excessive erosion:
If yes to any, explain:
Entry Gate Present:
  Gate locked on arrival:
Gate locked on departure:
Is spill or discharge of drilling, completion or produced fluids present:
 
If yes, did spill or discharge of drilling, completion or produced fluids occur or travel off the well pad:
(If yes, complete FIR 5)
Compliance Summary Remarks:
Well is in T/A status, compressor is not running, containment ring does not have a liner, no containment for 200 gal used oil tank, plumbing to used oil tank is leaking oil onto ground, excessive vegetation over location, but location has been sprayed for weed control. No enforcement at this time.MP

Inspected by: DAYMON BLOUNT   Date:  3/2/2020 11:08:00 AM
Review for NNC or NOV:
If yes, check one
Ref #: Date: 3/4/2020
ADEQ referral:
Date of referral:  __________