FIR 1 - INSPECTION REPORT

Permit Holder: Max Extract Technologies, LLC Well Name/No: ES 11609 Permit: 26458
Lease Name: ES 11609 1-4 Sec: 4 Twp: 11N Range 26W
GPS Well Location: Latitude: 35.65163 Longitude: -93.75591 Field: ROCK CREEK  
Lease/Tank Battery: Latitude: 35.65161 Longitude: 93.75594 County: FRANKLIN  
Entrance from nearest 911 address, public street or highway Low Bridge Road (US Forestry Road)
Status:
Well equipment operational: Equipment plumbed properly: Excess equipment on lease:
Signs: At lease entrance:
At tank battery:
At well:
Signage compliance:

NoTypeConstructionSizeLeaksRemarks
1Fluids TankFiberglassOther Size 10' round x 7' h = 98 bbls
2SeparatorSteel Welded   

Tank Containment:
Dimensions: Length: 24 Width: 25 Diameter: 0 Height: 1.25 Capacity (bbls): 134
Capacity compliance: Breaches/Erosion: Excessive vegetation present: Compliance agreement:
Containment Conditions: Fluids Present:
Well Site Compressor:
Is it in compliance?
Trash/Debris:
Use as storage area:
Unusual equipment:
Excessive erosion:
If yes to any, explain:
Entry Gate Present:
  Gate locked on arrival:
Gate locked on departure:
Is spill or discharge of drilling, completion or produced fluids present:
 
If yes, did spill or discharge of drilling, completion or produced fluids occur or travel off the well pad:
(If yes, complete FIR 5)
Compliance Summary Remarks:
No production reported since 08/2019, compressor has been removed for over a year, heavy oil in produced water tank, a two liter plastic bottle has been taped to tank drain for over a year and half, produced water tank has a constant leak of oil and fluids around plastic bottle taped on drain, public complaints have been filed on well and leaking tank.

Inspected by: DAYMON BLOUNT   Date:  2/10/2022 12:34:00 PM
Review for NNC or NOV:
If yes, check one
Ref #: Date: __________
ADEQ referral:
Date of referral:  __________