FIR 1 - INSPECTION REPORT

Permit Holder: Lyons & Lyons, Inc Well Name/No: Stengel Permit: 25684
Lease Name: Stengel 1 Sec: 27 Twp: 8N Range 27W
GPS Well Location: Latitude: 35.33241 Longitude: -93.84968 Field: AETNA  
Lease/Tank Battery: Latitude: 35.33257 Longitude: 93.85021 County: FRANKLIN  
Entrance from nearest 911 address, public street or highway Sheep Farm Road
Status:
Well equipment operational: Equipment plumbed properly: Excess equipment on lease:
Signs: At lease entrance:
At tank battery:
At well:
Signage compliance:

NoTypeConstructionSizeLeaksRemarks
1Fluids TankFiberglassOther Size 10' round x 7' h = 98 bbls
2Fluids TankOther TypesOther Size 4' x 4' x 4' plastic tote = 11 bbls (with dirt containment)
3SeparatorSteel Welded   

Tank Containment:
Dimensions: Length: 24 Width: 21 Diameter: 0 Height: 1 Capacity (bbls): 90
Capacity compliance: Breaches/Erosion: Excessive vegetation present: Compliance agreement:
Containment Conditions: Fluids Present:
Well Site Compressor:
Is it in compliance?
Trash/Debris:
Use as storage area:
Unusual equipment:
Excessive erosion:
If yes to any, explain: Several underground plumbing lines are leaking, several areas of oil and fluids actively bubbling up trough gravel. Used oil filters have been thrown onto ground.
Entry Gate Present:
  Gate locked on arrival:
Gate locked on departure:
Is spill or discharge of drilling, completion or produced fluids present:
 
If yes, did spill or discharge of drilling, completion or produced fluids occur or travel off the well pad:
(If yes, complete FIR 5)
Compliance Summary Remarks:
Producing, well is methanol injected, compressor is running, excessive vegetation inside containment and over location, dirt containment has eroded to less than tank capacity, large areas of location are covered with oil from active plumbing leaks. Operator contacted. Issues resolved.MP

Inspected by: DAYMON BLOUNT   Date:  12/1/2020 1:29:00 PM
Review for NNC or NOV:
If yes, check one
Ref #: Date: __________
ADEQ referral:
Date of referral:  __________