FIR 1 - INSPECTION REPORT

Permit Holder: Camterra Resources, Inc Well Name/No: UAFS Permit: 40463
Lease Name: UAFS 1-14D Sec: 14 Twp: 8N Range 32W
GPS Well Location: Latitude: 35.38106 Longitude: -94.36808 Field: MASSARD  
Lease/Tank Battery: Latitude: 0 Longitude: 0 County: SEBASTIAN  
Entrance from nearest 911 address, public street or highway Kinkead Ave
Status:
Well equipment operational: Equipment plumbed properly: Excess equipment on lease:
Signs: At lease entrance:
At tank battery:
At well:
Signage compliance:

NoTypeConstructionSizeLeaksRemarks
1Fluids TankFiberglass500 10' round x 7' h = 98 bbls
2Fluids TankFiberglassOther Size 15 bbl tank at dehy unit
3Dehy UnitSteel Bolted   
4Heater TreaterSteel Bolted   
5SeparatorSteel Welded   
6SeparatorSteel Welded   

Tank Containment:
Dimensions: Length: 0 Width: 0 Diameter: 20 Height: 2.33 Capacity (bbls): 130
Capacity compliance: Breaches/Erosion: Excessive vegetation present: Compliance agreement:
Containment Conditions: Fluids Present:
Well Site Compressor:
Is it in compliance?
Trash/Debris:
Use as storage area:
Unusual equipment:
Excessive erosion:
If yes to any, explain:
Entry Gate Present:
  Gate locked on arrival:
Gate locked on departure:
Is spill or discharge of drilling, completion or produced fluids present:
 
If yes, did spill or discharge of drilling, completion or produced fluids occur or travel off the well pad:
(If yes, complete FIR 5)
Compliance Summary Remarks:
Re-inspect as per Mike Passmore, DPM, (x2) showing 57 MCF 24 hour flow on upper tubing and 298 MCF 24 hour flow on main meter, compressor is running, leaking drain plug for produced water tank has been plugged, containment is still not 1 1/2 times tank capacity, clean location. Pumper removed vent plug in containment tank today to bring tank and containment back into compliance. No enforcement.MP

Inspected by: DAYMON BLOUNT   Date:  11/4/2015 12:00:00 AM
Review for NNC or NOV:
If yes, check one
Ref #: Date: 11/4/2015
ADEQ referral:
Date of referral:  __________