FIR 1 - INSPECTION REPORT

Permit Holder: Hanna Oil and Gas Company Well Name/No: Creekmore-Lake Permit: 36802
Lease Name: Creekmore-Lake 1-1 Sec: 1 Twp: 7N Range 29W
GPS Well Location: Latitude: 35.31708 Longitude: -94.02729 Field: VESTA  
Lease/Tank Battery: Latitude: 35.31714 Longitude: 94.02749 County: FRANKLIN  
Entrance from nearest 911 address, public street or highway North Rattlesnake Road
Status:
Well equipment operational: Equipment plumbed properly: Excess equipment on lease:
Signs: At lease entrance:
At tank battery:
At well:
Signage compliance:

NoTypeConstructionSizeLeaksRemarks
1Fluids TankFiberglassOther Size 10' round x 7' h = 98 bbls (holes at 49" = 57 bbls)
2Fluids TankFiberglassOther Size 5 bbl tank at dehy unit
3Dehy UnitSteel Bolted   
4SeparatorSteel Welded   
5SeparatorSteel Welded   

Tank Containment:
Dimensions: Length: 0 Width: 0 Diameter: 21 Height: 1.5 Capacity (bbls): 93
Capacity compliance: Breaches/Erosion: Excessive vegetation present: Compliance agreement:
Containment Conditions: Fluids Present:
Well Site Compressor:
Is it in compliance?
Trash/Debris:
Use as storage area:
Unusual equipment:
Excessive erosion:
If yes to any, explain:
Entry Gate Present:
  Gate locked on arrival:
Gate locked on departure:
Is spill or discharge of drilling, completion or produced fluids present:
 
If yes, did spill or discharge of drilling, completion or produced fluids occur or travel off the well pad:
(If yes, complete FIR 5)
Compliance Summary Remarks:
Producing, well is equipped with H2S scavenger, compressor is running, containment liner is completely rotted, moderate oil spilled outside of containment, an overflowing oil bucket is sitting on ground outside containment, sign at entry gate is blank. Operator contacted. No enforcement at this time.MP

Inspected by: DAYMON BLOUNT   Date:  10/5/2020 9:02:00 AM
Review for NNC or NOV:
If yes, check one
Ref #: Date: __________
ADEQ referral:
Date of referral:  __________